The solution to the challenge of increasing efficiencies and reducing waste consisted of dozens of engineering, technical and organisational actions and changes, rather than a single solution explains John D'Arcy, Consultant with Newton. ‘Firstly, we implemented a system whereby problems were quantified and then prioritised by cash value to the business, thus ensuring that our limited resources were always directed towards our most important problems.’
The two person Newton team was embedded within shop floor teams, working alongside operators and engineers. Adam Cleevely, Consultant with Newton, was impressed with the proactive attitude displayed by the team at Frederick’s ‘Frequently, problems briefly discussed in the workshop in the evening would have been completed by the next morning. The project resulted in solving numerous problems previously considered to be ‘the nature of the beast’, and therefore unsolvable’. We were able to complement the engineering skills on site, develop problem solving skills within engineering and production and ensure that the limited resource available was always working on the business critical problems, not just fire-fighting.’ A major challenge facing the team was increasing output on a choc-ice line. ‘The choc-ice line presented many problems’ explains Adam Cleevely ‘The line relied on high availability of 5 coupled machines, all of which were under-performing’. A particular problem was the case packing machine, which would stop for a myriad of reasons, up to 20 times an hour, and was frequently the largest contributor to rework that was having a significant impact on the efficiency of the overall machine. Developing accumulation before the case packer decoupled this part of the line and alone increased efficiencies by 9%. Installing the accumulation made clearer the issues with upstream machines and by methodically studying these, upwards of 50 permanent changes were made to improve performance. An example of the benefit of these studies concerned the wrapper machine. The wrapper was the largest individual contributor to waste and again beset by numerous small problems. 1 hour studies were carried out at the wrapper in-feed and out-feed to identify the largest causes to waste and downtime One by one, guides were redesigned, timings were perfected and the uniformity of product to the wrapper was improved. 15 improvements reduced the cost of waste and downtime due to the wrapper by 73%.
‘Frederick’s had technical issues common across the FMCG sector’ continues D’Arcy. ‘All lines suffered from numerous short duration high frequency downtime and waste problems. On one line, over 15% of waste was eliminated by monitoring the pattern of failure on 504 repeating moulds. Once we had found the faulty moulds, the problem was easily identified, and rectified over a weekend. The whole team was extremely satisfied to see the improvement in the figures continue week by week.’
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